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| NPDID wellbore: | 1512 | |
| Well name: | 2/7-19 | |
| Drilling operator name: | Phillips Petroleum Company Norway | |
| Geodetic datum: | ED50 | |
| Coordinates: | 56° 20` 19.10`` N | 3° 6` 12.20`` E |
| UTM coordinates: | 6243913.56 N | 506391.96 E |
| UTM zone: | 31 | |
| Drilled in production licence: | 018 | |
| Area: | NORTH SEA | |
| Discovery: | 2/7-19 | |
| Field: | NOT YET DEVELOPED | |
| Drill permit: | 262-L2 | |
| Drilling facility: | ROSS ISLE | |
| Drilling days: | 59 | |
| Wellbore entry date: | 15.01.1990 | |
| Wellbore completion date: | 14.03.1990 | |
| Reentry activity: | TESTING | |
| Original wellbore purpose: | WILDCAT | |
| Wellbore purpose: | WILDCAT | |
| Wellbore status: | P&A | |
| Wellbore contents: | OIL | |
| Discovery wellbore: | NO | |
| Formation/age with hydrocarbons 1: | ULA FM / LATE JURASSIC | |
| Seismic location: | PG 030615- SP. 12 | |
| Kelly bushing elevation (KB) [m]: | 22 | |
| Water depth [m]: | 73 | |
| Total Depth (MD) [m]: | 4873 | |
| Final vertical depth (TVD) [m]: | 4873 | |
| Max inclination [°]: | 3.40 | |
| Bottom hole temperature [°C]: | 179 | |
| Oldest penetrated age: | LATE PERMIAN | |
| Oldest penetrated formation: | ZECHSTEIN GP | |
| Note: All depths, except the water depth, are relative to kelly bushing (RKB) | ||
General
Well 2/7-19 R is a re-entry of well 2/7-19, which was drilled in 1980/81 by the semi-submersible Borgsten Dolphin. The well encountered gas in Early Cretaceous sandstones, but was suspended in February 1981 due to a BOP system that was not rated to allow a DST test to be performed. RFT tests measurements indicated a possible wellhead pressure of 11200 psi, while the BOP was rated to 10000 psi. A 7" liner was run to a depth of 4839 m and cemented, but not perforated. The purpose of the re-entry was to test 43 m of gross pay distributed in four sand lenses from 4712 to 4839 m. The DST test was designed such that it would be possible to keep the well for future production if flow rates were commercial.
Operations and results
Wildcat well 2/7-19 was re-entered (2/7-19 R) with the semi-submersible installation Ross Isle on 15 January 1990.
During drilling of the 2/7-19 well, only gas was encountered. The test in the re-entry showed that the reservoir rocks were tight, but a positive feature was that oil was encountered during testing. The test confirmed the earlier anticipated formation pressure of 860 to 895 bar.
The well was permanently abandoned on 14 March 1990 as an oil appraisal.
Testing
One DST test was performed from four sand lenses in the intervals 4712 - 4727 m, 4762 - 4783 m (Ula Formation), 4800 - 4818 m Ula/Bryne Formations), and 4830 - 4838 m (Bryne Formation). The total net pay in the perforated sections was 23 m. After acid treatment the well produced hydrocarbons at a rate of 34.8 Sm3 oil and 15631 Sm3 gas /d through an 11.91 mm choke. The CO2 content of the separator gas was 4.4%. The GOR was 449 Sm3/Sm3 but this figure is uncertain due to slugging of the well and poor rate measurements. The matrix/acid job performed was not effective. The stable shut-in temperature at 4628 m (gauge depth) was 169 deg C, while maximum recorded flowing temperature was 172 deg C. It was not established which of the four perforated sections that contributed to the flow.
No cuttings in this wellbore.
No cores in this wellbore.
No scanned core photos available
| Test type: | Bottle test number: | Bottle interval [m]: | Fluid type: | Test date and time: |
|---|---|---|---|---|
| DST | DST1 | 4838.400 - 4711.600 | 1990.02.16 00:00 |
| Depth MD [m] | Mud weight [g/cm3] | Visc. [MPa.s] | Yield [pnt Pa.] | Mud type | Date measured |
|---|---|---|---|---|---|
| 363 | 1.32 | 8.0 | 16.8 | WATER BASED | 1990.03.12 |
| 1106 | 1.32 | 5.0 | 6.7 | WATER BASED | 1990.03.09 |
| 1106 | 1.32 | 5.0 | 6.7 | WATER BASED | 1990.03.12 |
| 3398 | 2.06 | 58.0 | 19.6 | OIL BASED | 1990.02.28 |
| 3398 | 1.82 | 10.0 | 19.2 | WATER BASED | 1990.03.02 |
| 3398 | 1.82 | 11.0 | 19.6 | WATER BASED | 1990.03.05 |
| 3398 | 1.82 | 10.0 | 18.2 | WATER BASED | 1990.03.05 |
| 3398 | 1.82 | 11.0 | 16.8 | WATER BASED | 1990.03.05 |
| 3398 | 1.82 | 10.0 | 16.8 | WATER BASED | 1990.03.06 |
| 3398 | 1.82 | 10.0 | 17.2 | WATER BASED | 1990.03.07 |
| 3398 | 1.68 | 8.0 | 12.9 | WATER BASED | 1990.03.08 |
| 3398 | 1.82 | 11.0 | 20.6 | WATER BASED | 1990.03.02 |
| 4544 | 2.04 | 53.0 | 9.6 | OIL BASED | 1990.02.28 |
| 4544 | 2.09 | 58.0 | 13.9 | OIL BASED | 1990.02.28 |
| 4544 | 2.06 | 58.0 | 19.6 | OIL BASED | 1990.02.28 |
| 4544 | 2.10 | 61.0 | 14.4 | OIL BASED | 1990.02.28 |
| 4718 | 2.04 | 52.0 | 10.5 | OIL BASED | 1990.02.22 |
| 4718 | 2.04 | 51.0 | 10.5 | OIL BASED | 1990.02.23 |
| 4862 | 2.05 | 33.0 | 10.1 | OIL BASED | 1990.02.05 |
| 4862 | 2.06 | 54.0 | 17.2 | OIL BASED | 1990.02.05 |
| 4862 | 2.05 | 52.0 | 12.4 | OIL BASED | 1990.02.05 |
| 4862 | 2.04 | 50.0 | 10.5 | OIL BASED | 1990.02.05 |
| 4862 | 2.04 | 49.0 | 13.4 | OIL BASED | 1990.02.06 |
| 4862 | 2.04 | 42.0 | 10.1 | OIL BASED | 1990.02.07 |
| 4862 | 2.04 | 51.0 | 13.4 | OIL BASED | 1990.02.08 |
| 4862 | 2.04 | 45.0 | 14.4 | OIL BASED | 1990.02.09 |
| 4862 | 2.10 | 46.0 | 12.9 | OIL BASED | 1990.02.12 |
| 4862 | 2.04 | 50.0 | 14.4 | OIL BASED | 1990.02.12 |
| 4862 | 2.04 | 43.0 | 12.0 | OIL BASED | 1990.02.13 |
| 4862 | 2.04 | 43.0 | 12.0 | OIL BASED | 1990.02.14 |
| 4862 | 2.01 | 48.0 | 8.6 | OIL BASED | 1990.02.15 |
| 4862 | 2.04 | 50.0 | 14.4 | OIL BASED | 1990.02.16 |
| 4862 | 2.04 | 49.0 | 13.4 | OIL BASED | 1990.02.19 |
| 4862 | 2.04 | 51.0 | 14.8 | OIL BASED | 1990.02.19 |
| 4862 | 2.04 | 51.0 | 11.0 | OIL BASED | 1990.02.20 |
| 4862 | 2.04 | 50.0 | 10.5 | OIL BASED | 1990.02.21 |
| 4862 | 2.04 | 43.0 | 12.0 | OIL BASED | 1990.02.12 |
| 4862 | 2.04 | 48.0 | 12.9 | OIL BASED | 1990.02.19 |
| Test no. | Test interval [m] | Choke size [mm] | Final shut in pressure [MPa] | Final flow pressure [MPa] | Bottom hole pressure [MPa] | Downhole temperature [°C] |
|---|---|---|---|---|---|---|
| 1.0 | 4711 - 4838 | 12.0 | 2.700 | 0 |
| Test no. | Oil [Sm3/day] | Gas [Sm3/day] | Oil grav. [g/cm3] | Gas grav. rel.air | GOR [m3/m3] |
|---|---|---|---|---|---|
| 1.0 | 35 | 15631 | 449 |
No logs available.
| Top depth [m] | Litostratigraphic unit |
|---|---|
| 95 | NORDLAND GP |
| 1527 | HORDALAND GP |
| 2984 | ROGALAND GP |
| 2984 | BALDER FM |
| 3001 | SELE FM |
| 3024 | LISTA FM |
| 3066 | VÅLE FM |
| 3127 | SHETLAND GP |
| 3127 | EKOFISK FM |
| 3185 | TOR FM |
| 3441 | HOD FM |
| 4052 | BLODØKS FM |
| 4078 | HIDRA FM |
| 4209 | CROMER KNOLL GP |
| 4209 | RØDBY FM |
| 4325 | SOLA FM |
| 4465 | ÅSGARD FM |
| 4583 | TYNE GP |
| 4583 | MANDAL FM |
| 4587 | FARSUND FM |
| 4690 | VESTLAND GP |
| 4690 | ULA FM |
| 4807 | BRYNE FM |
| 4837 | ZECHSTEIN GP |
No composite log presently available.
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