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Exploration wellbore: 2/7-19 R

General information

NPDID wellbore: 1512
Well name: 2/7-19
Drilling operator name: Phillips Petroleum Company Norway
Geodetic datum: ED50
Coordinates: 56° 20` 19.10`` N 3° 6` 12.20`` E
UTM coordinates: 6243913.56 N 506391.96 E
UTM zone: 31
Drilled in production licence: 018
Area: NORTH SEA
Discovery:2/7-19
Field:NOT YET DEVELOPED
Drill permit: 262-L2
Drilling facility:ROSS ISLE
Drilling days: 59
Wellbore entry date: 15.01.1990
Wellbore completion date: 14.03.1990
Reentry activity:TESTING
Original wellbore purpose: WILDCAT
Wellbore purpose: WILDCAT
Wellbore status: P&A
Wellbore contents: OIL
Discovery wellbore: NO
Formation/age with hydrocarbons 1:ULA FM / LATE JURASSIC
Seismic location: PG 030615- SP. 12
Kelly bushing elevation (KB) [m]: 22
Water depth [m]: 73
Total Depth (MD) [m]: 4873
Final vertical depth (TVD) [m]: 4873
Max inclination [°]: 3.40
Bottom hole temperature [°C]: 179
Oldest penetrated age: LATE PERMIAN
Oldest penetrated formation: ZECHSTEIN GP
Note: All depths, except the water depth, are relative to kelly bushing (RKB)

Wellbore history

General

Well 2/7-19 R is a re-entry of well 2/7-19, which was drilled in 1980/81 by the semi-submersible Borgsten Dolphin. The well encountered gas in Early Cretaceous sandstones, but was suspended in February 1981 due to a BOP system that was not rated to allow a DST test to be performed. RFT tests measurements indicated a possible wellhead pressure of 11200 psi, while the BOP was rated to 10000 psi. A 7" liner was run to a depth of 4839 m and cemented, but not perforated. The purpose of the re-entry was to test 43 m of gross pay distributed in four sand lenses from 4712 to 4839 m. The DST test was designed such that it would be possible to keep the well for future production if flow rates were commercial.

Operations and results

Wildcat well 2/7-19 was re-entered (2/7-19 R) with the semi-submersible installation Ross Isle on 15 January 1990.

During drilling of the 2/7-19 well, only gas was encountered. The test in the re-entry showed that the reservoir rocks were tight, but a positive feature was that oil was encountered during testing. The test confirmed the earlier anticipated formation pressure of 860 to 895 bar.

The well was permanently abandoned on 14 March 1990 as an oil appraisal.

Testing

One DST test was performed from four sand lenses in the intervals 4712 - 4727 m, 4762 - 4783 m (Ula Formation), 4800 - 4818 m Ula/Bryne Formations), and 4830 - 4838 m (Bryne Formation). The total net pay in the perforated sections was 23 m. After acid treatment the well produced hydrocarbons at a rate of 34.8 Sm3 oil and 15631 Sm3 gas /d through an 11.91 mm choke. The CO2 content of the separator gas was 4.4%. The GOR was 449 Sm3/Sm3 but this figure is uncertain due to slugging of the well and poor rate measurements. The matrix/acid job performed was not effective. The stable shut-in temperature at 4628 m (gauge depth) was 169 deg C, while maximum recorded flowing temperature was 172 deg C. It was not established which of the four perforated sections that contributed to the flow.

Cuttings available at the NPD

No cuttings in this wellbore.

Cores available at the NPD

No cores in this wellbore.

Scanned core photos

No scanned core photos available

Palynological slides available at the NPD

Oil samples available at the NPD

Test type: Bottle test number: Bottle interval [m]: Fluid type: Test date and time:
DST DST1 4838.400 - 4711.600 1990.02.16 00:00

Casing and leak-off tests

No data available.

Mud

Depth MD [m] Mud weight [g/cm3] Visc. [MPa.s] Yield [pnt Pa.] Mud type Date measured
363 1.32 8.0 16.8 WATER BASED 1990.03.12
1106 1.32 5.0 6.7 WATER BASED 1990.03.09
1106 1.32 5.0 6.7 WATER BASED 1990.03.12
3398 2.06 58.0 19.6 OIL BASED 1990.02.28
3398 1.82 10.0 19.2 WATER BASED 1990.03.02
3398 1.82 11.0 19.6 WATER BASED 1990.03.05
3398 1.82 10.0 18.2 WATER BASED 1990.03.05
3398 1.82 11.0 16.8 WATER BASED 1990.03.05
3398 1.82 10.0 16.8 WATER BASED 1990.03.06
3398 1.82 10.0 17.2 WATER BASED 1990.03.07
3398 1.68 8.0 12.9 WATER BASED 1990.03.08
3398 1.82 11.0 20.6 WATER BASED 1990.03.02
4544 2.04 53.0 9.6 OIL BASED 1990.02.28
4544 2.09 58.0 13.9 OIL BASED 1990.02.28
4544 2.06 58.0 19.6 OIL BASED 1990.02.28
4544 2.10 61.0 14.4 OIL BASED 1990.02.28
4718 2.04 52.0 10.5 OIL BASED 1990.02.22
4718 2.04 51.0 10.5 OIL BASED 1990.02.23
4862 2.05 33.0 10.1 OIL BASED 1990.02.05
4862 2.06 54.0 17.2 OIL BASED 1990.02.05
4862 2.05 52.0 12.4 OIL BASED 1990.02.05
4862 2.04 50.0 10.5 OIL BASED 1990.02.05
4862 2.04 49.0 13.4 OIL BASED 1990.02.06
4862 2.04 42.0 10.1 OIL BASED 1990.02.07
4862 2.04 51.0 13.4 OIL BASED 1990.02.08
4862 2.04 45.0 14.4 OIL BASED 1990.02.09
4862 2.10 46.0 12.9 OIL BASED 1990.02.12
4862 2.04 50.0 14.4 OIL BASED 1990.02.12
4862 2.04 43.0 12.0 OIL BASED 1990.02.13
4862 2.04 43.0 12.0 OIL BASED 1990.02.14
4862 2.01 48.0 8.6 OIL BASED 1990.02.15
4862 2.04 50.0 14.4 OIL BASED 1990.02.16
4862 2.04 49.0 13.4 OIL BASED 1990.02.19
4862 2.04 51.0 14.8 OIL BASED 1990.02.19
4862 2.04 51.0 11.0 OIL BASED 1990.02.20
4862 2.04 50.0 10.5 OIL BASED 1990.02.21
4862 2.04 43.0 12.0 OIL BASED 1990.02.12
4862 2.04 48.0 12.9 OIL BASED 1990.02.19

Drill stem test (intervals and pressures)

Test no. Test interval [m] Choke size [mm] Final shut in pressure [MPa] Final flow pressure [MPa] Bottom hole pressure [MPa] Downhole temperature [°C]
1.0 4711 - 4838 12.0 2.700 0

Drill Stem Test (recovery)

Test no. Oil [Sm3/day] Gas [Sm3/day] Oil grav. [g/cm3] Gas grav. rel.air GOR [m3/m3]
1.0 35 15631 449

Available logs

No logs available.

Lithostratigraphy

Top depth [m] Litostratigraphic unit
95 NORDLAND GP
1527 HORDALAND GP
2984 ROGALAND GP
2984 BALDER FM
3001 SELE FM
3024 LISTA FM
3066 VÅLE FM
3127 SHETLAND GP
3127 EKOFISK FM
3185 TOR FM
3441 HOD FM
4052 BLODØKS FM
4078 HIDRA FM
4209 CROMER KNOLL GP
4209 RØDBY FM
4325 SOLA FM
4465 ÅSGARD FM
4583 TYNE GP
4583 MANDAL FM
4587 FARSUND FM
4690 VESTLAND GP
4690 ULA FM
4807 BRYNE FM
4837 ZECHSTEIN GP

Composite log

No composite log presently available.

Geochemical information

File 1 (Format:PDF. Size: 0.207 Mb )
File 2 (Format:PDF. Size: 0.982 Mb )
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Documents reported by the licencees (period for duty of secrecy expired)

No documents presently available.



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