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| NPDID wellbore: | 1667 | |
| Well name: | 2/1-9 | |
| Drilling operator name: | BP Norway Limited U.A. | |
| Geodetic datum: | ED50 | |
| Coordinates: | 56° 51` 37.77`` N | 3° 5` 04.77`` E |
| UTM coordinates: | 6302000.77 N | 505162.30 E |
| UTM zone: | 31 | |
| Drilled in production licence: | 019-B | |
| Area: | NORTH SEA | |
| Discovery: | 2/1-9 GYDA SØR | |
| Field: | GYDA | |
| Drill permit: | 676-L | |
| Drilling facility: | ROSS ISLE | |
| Drilling days: | 83 | |
| Wellbore entry date: | 15.04.1991 | |
| Wellbore completion date: | 06.07.1991 | |
| Original wellbore purpose: | APPRAISAL | |
| Wellbore purpose: | WILDCAT | |
| Wellbore status: | P&A | |
| Wellbore contents: | OIL | |
| Discovery wellbore: | YES | |
| Formation/age with hydrocarbons 1: | ULA FM / LATE JURASSIC | |
| Seismic location: | X-OVER 3D LINE 560 AND X-LINE 570 | |
| Kelly bushing elevation (KB) [m]: | 23 | |
| Water depth [m]: | 66 | |
| Total Depth (MD) [m]: | 4289 | |
| Final vertical depth (TVD) [m]: | 4289 | |
| Max inclination [°]: | 2.20 | |
| Bottom hole temperature [°C]: | 160 | |
| Oldest penetrated age: | LATE PERMIAN | |
| Oldest penetrated formation: | ZECHSTEIN GP | |
| Note: All depths, except the water depth, are relative to kelly bushing (RKB) | ||
General
Well 2/1-9 was drilled on the Gyda South structure, a fault/dip closure in the Late Jurassic fairway on the eastern flank of the Central Graben, 6 km south of the Gyda Field. The main objective of the well was to test the Late Jurassic "Gyda sandstone" (Ula Formation) target and prove a volume of oil that was commercial as a tie back development to the Gyda platform. Secondary reservoir potential existed in both the Middle Jurassic and in the uppermost part of the Triassic. Estimated TD was 4275 m TVD RKB.
Operations and results
Appraisal well 2/1-9 was spudded with the semi submersible rig Ross Isle 15 March 1991 and drilled to TD at 4298 m in the late Permian Zechstein Group. No significant problems were encountered in the operations. No shallow gas was detected. The well was drilled with seawater and high viscosity slugs down to 900 m, and with Aquamul ether-based invert emulsion mud system from 900 m to TD.
A 59 m Forties Formation sandstone sequence was encountered at 2923 m in the Late Paleocene and another ca 30 m thick sandstone sequence at 3025 m within the Lista Formation. Top Mandal Formation was encountered at 4013.5 m, 10.5m deeper than predicted. Top Ula Formation was encountered hydrocarbon bearing from 4048 to 4209 m, which was 111 m thicker than expected. The OWC was interpreted from logs to be at 4137.0 m, while the cores taken had good oil shows all through the cored section, i.e. down to 4153 m. No reservoir sections were encountered in the Middle Jurassic. No Triassic sediments were penetrated by the well.
Five cores were cut continuously from 4019 m to 4153 m with 100% recovery. Core 1 covered the lower part of the Mandal, Farsund, and the upper part of the Ula Formation. Cores 2, 3, 4 and 5 were cut in the Ula Formation. Good oil shows was observed throughout the cored section of the Ula sandstone. RFT fluid samples were taken at 4088.7 m (oil), 4137.0 m (oil), 4151 (water), and 4177 m (water).
Well 2/1-9 was considered a potential water injector for the Gyda South discovery, and to be sidetracked up-dip as a producer. A full evaluation of the DST and PVT data would be performed together with a geological remapping and evaluation of the discovery. The well was thus suspended on 6 July 1991, as an oil discovery. It would be re-entered later, after the above evaluations had been completed.
Testing
One DST was run in the interval 4078 - 4108 m and resulted in an oil rate of 166 Sm3 oil/day through a 32/64" choke. The gas rate was 91180 Sm3/day and the water rate was 120 Sm3/day. The GOR was 548 Sm3/Sm3 and the oil gravity was 43 deg API. Due to the presence of H2S the lower part of the Ula Formation was not tested.
No cuttings in this wellbore.
Core length [m]: 133.54
| Core number | Interval |
|---|---|
| 1 | 4019-4046 |
| 2 | 4046-4074 |
| 3 | 4074-4102 |
| 4 | 4102-4124.45 |
| 5 | 4125-4153 |
No palynological slides in this wellbore.
| Test type: | Bottle test number: | Bottle interval [m]: | Fluid type: | Test date and time: |
|---|---|---|---|---|
| DST | 0.000 - 0.000 | 00:00 | ||
| DST | DST1 | 4078.000 - 4108.000 | 1991.06.14 00:00 |
| Type | Casing diam. [inch] | Depth below KB [m] | Hole diam. [inch] | Hole depth below KB [m] | Lot mud eqv. [g/cm3] |
|---|---|---|---|---|---|
| CONDUCTOR | 30 | 164.0 | 36 | 166.0 | |
| INTERM. | 20 | 895.0 | 26 | 897.0 | 1.74 |
| INTERM. | 13 3/8 | 2893.0 | 17 1/2 | 2896.0 | 2.03 |
| INTERM. | 9 5/8 | 3938.0 | 12 1/4 | 3940.0 | 2.15 |
| LINER | 7 | 4275.0 | 8 1/2 | 4289.0 |
| Depth MD [m] | Mud weight [g/cm3] | Visc. [MPa.s] | Yield [pnt Pa.] | Mud type | Date measured |
|---|---|---|---|---|---|
| 415 | OIL BASED | ||||
| 426 | 1.57 | 42.0 | OIL BASED | ||
| 900 | 1.04 | WATER BASED | |||
| 961 | 1.20 | 31.0 | WATER BASED | ||
| 1583 | 1.39 | 49.0 | WATER BASED | ||
| 2153 | 1.60 | 72.0 | WATER BASED | ||
| 2474 | 1.60 | 64.0 | WATER BASED | ||
| 2529 | 1.60 | 74.0 | WATER BASED | ||
| 2682 | 1.60 | 73.0 | WATER BASED | ||
| 2874 | 1.60 | 71.0 | WATER BASED | ||
| 2901 | 1.60 | 77.0 | WATER BASED | ||
| 3018 | 1.60 | 69.0 | WATER BASED | ||
| 3114 | 1.60 | 68.0 | WATER BASED | ||
| 3173 | 1.60 | 7.7 | WATER BASED | ||
| 3193 | 1.60 | 57.0 | WATER BASED | ||
| 3243 | 1.60 | 60.0 | WATER BASED | ||
| 3253 | 1.60 | 68.0 | WATER BASED | ||
| 3318 | 1.60 | 76.0 | WATER BASED | ||
| 3413 | 1.60 | 79.0 | WATER BASED | ||
| 3610 | 1.60 | 80.0 | WATER BASED | ||
| 3775 | 1.73 | 85.0 | WATER BASED | ||
| 3847 | 1.73 | 77.0 | WATER BASED | ||
| 3910 | 1.73 | 82.0 | OIL BASED | ||
| 3947 | 1.73 | 91.0 | OIL BASED | ||
| 3967 | 1.72 | 82.0 | OIL BASED | ||
| 4019 | 1.62 | 51.0 | OIL BASED | ||
| 4039 | 1.56 | 49.0 | OIL BASED | ||
| 4074 | 1.56 | 47.0 | OIL BASED | ||
| 4102 | 1.57 | 53.0 | OIL BASED | ||
| 4125 | .14 | 53.0 | OIL BASED | ||
| 4153 | 1.57 | 53.0 | OIL BASED | ||
| 4240 | 1.58 | 56.0 | OIL BASED | ||
| 4289 | 1.59 | 72.0 | OIL BASED |
| Test no. | Test interval [m] | Choke size [mm] | Final shut in pressure [MPa] | Final flow pressure [MPa] | Bottom hole pressure [MPa] | Downhole temperature [°C] |
|---|---|---|---|---|---|---|
| 1.0 | 4078 - 4108 | 17.4 | 7.000 | 23.600 | 0 |
| Test no. | Oil [Sm3/day] | Gas [Sm3/day] | Oil grav. [g/cm3] | Gas grav. rel.air | GOR [m3/m3] |
|---|---|---|---|---|---|
| 1.0 | 165 | 90577 | 549 |
| Log type | Intervals logged [m] |
|---|---|
| MWD - RWD | 88 - 4289 |
| DIL LLS GR | - 3954 |
| CBL VDL CCL GR | 2040 - 2895 |
| CST GR | 3500 - 3947 |
| DIL SDT GR | 3945 - 4298 |
| LDL CNL NGT | 3945 - 4298 |
| OBDT GR | 3945 - 4298 |
| RFT GR SAMPLE | 4049 - 4243 |
| RFT SAMPLE | 4151 - 4151 |
| RFT SAMPLE | 4177 - 4177 |
| RFT SAMPLE | 4088 - 4088 |
| CST GR | 3957 - 4288 |
| CBL VDL CCL GR | 3761 - 4249 |
| VELOCITY | 500 - 4213 |
| JUNK BASKET CCL | 3980 - 3980 |
| JUNK BASKET CCL | 4250 - 4250 |
| PERM PACKER | 4003 - 4003 |
| GR CCL | 2700 - 2700 |
| GR CCL | 4003 - 4003 |
| GR CCL | 4150 - 4150 |
| ENERJET CCL | 4078 - 4093 |
| ENERJET CCL | 4093 - 4108 |
| Top depth [m] | Litostratigraphic unit |
|---|---|
| 89 | NORDLAND GP |
| 1814 | HORDALAND GP |
| 2898 | ROGALAND GP |
| 2898 | BALDER FM |
| 2915 | SELE FM |
| 2923 | FORTIES FM |
| 2982 | LISTA FM |
| 3055 | VIDAR FM |
| 3143 | LISTA FM |
| 3158 | VÅLE FM |
| 3168 | SHETLAND GP |
| 3168 | EKOFISK FM |
| 3256 | TOR FM |
| 3617 | HOD FM |
| 3765 | BLODØKS FM |
| 3783 | HIDRA FM |
| 3800 | CROMER KNOLL GP |
| 3800 | RØDBY FM |
| 3838 | SOLA FM |
| 3852 | TUXEN FM |
| 3867 | ÅSGARD FM |
| 4014 | TYNE GP |
| 4014 | MANDAL FM |
| 4034 | FARSUND FM |
| 4048 | VESTLAND GP |
| 4048 | ULA FM |
| 4257 | BRYNE FM |
| 4289 | ZECHSTEIN GP |
No composite log presently available.
| File 1 | (Format:PDF. Size: 0.319 Mb ) |
| File 2 | (Format:PDF. Size: 0.946 Mb ) |
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No documents presently available.
| WDSS_General_Information | (Format:PDF. Size: 1.430 Mb ) |
| WDSS_completion_log | (Format:PDF. Size: 0.212 Mb ) |
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You need an ACROBAT reader from ADOBE to display the reports in pdf format. |