|
The NPD's Fact-pages |
|
Generated 11.02.2012 |
|
After more than 10 years as a fact provider NPDs FactPages version 1 will be shut down in Dec. 2011.
Start using FactPages version 2 now! See also FactPages version 2 Quick Reference' If you have any questions or comments please send an e-mail to FactWEB@npd.no. |
| NPDID wellbore: | 1956 | |
| Well name: | 2/4-16 | |
| Drilling operator name: | Saga Petroleum ASA | |
| Geodetic datum: | ED50 | |
| Coordinates: | 56° 40` 37.23`` N | 3° 9` 02.07`` E |
| UTM coordinates: | 6281583.13 N | 509226.66 E |
| UTM zone: | 31 | |
| Drilled in production licence: | 146 | |
| Area: | NORTH SEA | |
| Drill permit: | 680-L2 | |
| Drilling facility: | TREASURE SAGA | |
| Drilling days: | 42 | |
| Wellbore entry date: | 04.06.1992 | |
| Wellbore completion date: | 15.07.1992 | |
| Original wellbore purpose: | WILDCAT | |
| Wellbore purpose: | WILDCAT | |
| Wellbore status: | JUNKED | |
| Wellbore contents: | SHOWS | |
| Discovery wellbore: | NO | |
| Seismic location: | BB-87-043A- SP.10870 | |
| Kelly bushing elevation (KB) [m]: | 26 | |
| Water depth [m]: | 68 | |
| Total Depth (MD) [m]: | 4973 | |
| Final vertical depth (TVD) [m]: | ||
| Max inclination [°]: | 3.10 | |
| Bottom hole temperature [°C]: | ||
| Oldest penetrated age: | MIDDLE JURASSIC | |
| Oldest penetrated formation: | BRYNE FM | |
| Note: All depths, except the water depth, are relative to kelly bushing (RKB) | ||
General
The licence area is located in a prolific area in the southern North Sea on the eastern margin of the Feda Graben. Well 2/4-16 was drilled on the eastern margin of the Feda Graben North of the Albuskjell and Ekofisk Fields in the North Sea. Geologically the area consists of three sub-platforms. These are separated by large NW-SE striking normal faults down-faulted to the southwest and stepping down to the Feda Graben in the southern part of the block. The 2/4-16 well is located in the centre of the licence area on the same down faulted segment as the blowout wells 2/4-13, -14 and -15. Well 2/4-16 was temporarily abandoned at 4996 m in the Middle Jurassic Bryne formation due to operational problems. The main objective of well 2/4-16 R was to penetrate the Middle Jurassic and through the Triassic sequence to test for possible hydrocarbon bearing sandstone sequences. The plan was to sidetrack just below the 7 5/8" casing shoe at 4892 m and if operation permitted, to penetrate the complete Triassic sequence and terminate the well in the Zechstein Group evaporites. Planned TD for the well was 5190 + 60 m. If no signs of salt/anhydrite, the maximum TD of the well should be 5250 m.
Operations and results
Well 2/4-16 was re-entered (2/4-16 R) with the semi-submersible installation Treasure Saga on 4 June 1992. The old hole was sidetracked between 4900 to 4930 m and drilled to 4973 m in the Middle Jurassic Bryne Formation where the well was terminated due to extremely high pore pressures in the range 2.16 - 2.17 EMW. One week was spent attempting to bleed off pressure with no success. Analysis of the bleed-off operation showed that it was impossible to reduce the high pore pressure. As the source of the extreme pore pressure is of unknown origin it was decided to stop further drilling and permanently abandon the well.
No conventional logs for formation evaluation were run. No cores were cut and no wire line fluid samples taken.
The well was permanently abandoned on 15 July 1992 as a dry well with shows.
Testing
No drill stem test was performed
No cuttings in this wellbore.
No cores in this wellbore.
No scanned core photos available
No palynological slides in this wellbore.
No oil samples available.
| Type | Casing diam. [inch] | Depth below KB [m] | Hole diam. [inch] | Hole depth below KB [m] | Lot mud eqv. [g/cm3] |
|---|---|---|---|---|---|
| LINER | 6 | 4882.0 | 7 5/8 | 4973.0 |
| Depth MD [m] | Mud weight [g/cm3] | Visc. [MPa.s] | Yield [pnt Pa.] | Mud type | Date measured |
|---|---|---|---|---|---|
| 110 | 1.85 | 21.0 | 8.0 | WATER BASED | 1992.07.15 |
| 110 | 1.85 | 21.0 | 8.0 | WATER BASED | 1992.07.15 |
| 110 | 1.85 | 21.0 | 8.0 | WATER BASED | 1992.07.16 |
| 4632 | 2.18 | 28.0 | 3.0 | WATER BASED | 1992.07.03 |
| 4632 | 2.18 | 28.0 | 3.0 | WATER BASED | 1992.07.07 |
| 4632 | 2.18 | 32.0 | 7.0 | WATER BASED | 1992.07.07 |
| 4632 | 1.80 | 21.0 | 7.0 | WATER BASED | 1992.07.08 |
| 4632 | 1.80 | 21.0 | 7.0 | WATER BASED | 1992.07.08 |
| 4632 | 1.77 | 21.0 | 7.0 | WATER BASED | 1992.07.10 |
| 4632 | 2.18 | 2728.0 | 3.0 | WATER BASED | 1992.07.07 |
| 4650 | 1.85 | 21.0 | 4.0 | WATER BASED | 1992.07.14 |
| 4650 | 1.85 | 20.0 | 5.0 | WATER BASED | 1992.07.14 |
| 4650 | 1.85 | 20.0 | 5.0 | WATER BASED | 1992.07.14 |
| 4903 | 2.14 | 33.0 | 3.0 | WATER BASED | 1992.06.16 |
| 4903 | 2.14 | 33.0 | 3.0 | WATER BASED | 1992.06.16 |
| 4915 | 2.14 | 32.0 | 6.0 | WATER BASED | 1992.06.16 |
| 4915 | 2.14 | 32.0 | 6.0 | WATER BASED | 1992.06.16 |
| 4927 | 2.14 | 28.0 | 3.0 | WATER BASED | 1992.06.16 |
| 4927 | 2.14 | 28.0 | 3.0 | WATER BASED | 1992.06.16 |
| 4930 | 2.14 | 26.0 | 2.0 | WATER BASED | 1992.06.18 |
| 4949 | 2.14 | 27.0 | 4.0 | WATER BASED | 1992.06.19 |
| 4954 | 2.14 | 26.0 | 2.0 | WATER BASED | 1992.06.19 |
| 4973 | 2.14 | 27.0 | 2.0 | WATER BASED | 1992.06.22 |
| 4973 | 2.14 | 27.0 | 3.0 | WATER BASED | 1992.06.22 |
| 4973 | 2.14 | 25.0 | 4.0 | WATER BASED | 1992.06.22 |
| 4973 | 2.14 | 29.0 | 3.0 | WATER BASED | 1992.06.23 |
| 4973 | 2.14 | 28.0 | 4.0 | WATER BASED | 1992.06.24 |
| 4973 | 2.16 | 32.0 | 5.0 | WATER BASED | 1992.06.26 |
| 4973 | 2.20 | 34.0 | 6.0 | WATER BASED | 1992.06.30 |
| 4973 | 2.20 | 34.0 | 8.0 | WATER BASED | 1992.06.30 |
| 4973 | 2.20 | 35.0 | 8.0 | WATER BASED | 1992.06.30 |
| 4973 | 2.17 | 35.0 | 11.0 | WATER BASED | 1992.06.30 |
| 4973 | 2.20 | 33.0 | 6.0 | WATER BASED | 1992.07.02 |
| 4973 | 2.20 | 33.0 | 7.0 | WATER BASED | 1992.07.02 |
| 4973 | 1.85 | 22.0 | 4.0 | WATER BASED | 1992.07.13 |
| 4973 | 2.19 | 35.0 | 12.0 | WATER BASED | 1992.06.30 |
No drill stem test in this wellbore.
No logs available.
| Top depth [m] | Litostratigraphic unit |
|---|---|
| 94 | NORDLAND GP |
| 833 | NO FORMAL NAME |
| 914 | NO FORMAL NAME |
| 1798 | HORDALAND GP |
| 3140 | ROGALAND GP |
| 3140 | BALDER FM |
| 3155 | SELE FM |
| 3189 | LISTA FM |
| 3238 | VIDAR FM |
| 3254 | LISTA FM |
| 3292 | VÅLE FM |
| 3317 | SHETLAND GP |
| 3317 | EKOFISK FM |
| 3435 | TOR FM |
| 3920 | HOD FM |
| 4575 | BLODØKS FM |
| 4598 | HIDRA FM |
| 4638 | CROMER KNOLL GP |
| 4638 | RØDBY FM |
| 4678 | TUXEN FM |
| 4714 | ÅSGARD FM |
| 4737 | TYNE GP |
| 4737 | MANDAL FM |
| 4770 | FARSUND FM |
| 4828 | HAUGESUND FM |
| 4877 | VESTLAND GP |
| 4877 | BRYNE FM |
No composite log presently available.
No geochemical data presently available. Regional geochemical studies which include data from this well may however be filed on a different well.
No documents presently available.