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| NPDID wellbore: | 4728 | |
| Well name: | 24/6-3 | |
| Drilling operator name: | Marathon Petroleum Norge AS | |
| Geodetic datum: | ED50 | |
| Coordinates: | 59° 34` 44.57`` N | 1° 54` 47.45`` E |
| UTM coordinates: | 6605187.76 N | 438610.00 E |
| UTM zone: | 31 | |
| Drilled in production licence: | 088-BS | |
| Area: | NORTH SEA | |
| Discovery: | 24/6-2 ALVHEIM | |
| Field: | ALVHEIM | |
| Drill permit: | 1054-L | |
| Drilling facility: | DEEPSEA BERGEN | |
| Drilling days: | 5 | |
| Wellbore entry date: | 18.04.2003 | |
| Wellbore completion date: | 22.04.2003 | |
| Original wellbore purpose: | APPRAISAL | |
| Wellbore purpose: | APPRAISAL | |
| Wellbore status: | JUNKED | |
| Wellbore contents: | DRY | |
| Discovery wellbore: | NO | |
| Seismic location: | line 484 & trace 4798- NH9601 | |
| Kelly bushing elevation (KB) [m]: | 23 | |
| Water depth [m]: | 121 | |
| Total Depth (MD) [m]: | 253 | |
| Final vertical depth (TVD) [m]: | 253 | |
| Max inclination [°]: | ||
| Bottom hole temperature [°C]: | ||
| Oldest penetrated age: | PLIOCENE | |
| Oldest penetrated formation: | NORDLAND GP | |
| Note: All depths, except the water depth, are relative to kelly bushing (RKB) | ||
General
Well 24/6-3 was designed to appraise the Kameleon 24/6-2 discovery made in 1998. The well objectives were: to verify the field wide extent of fluid and gas contacts, eliminate geologic risk associated with the Boa structure, provide additional time-depth control, provide gas, oil and water samples, and to test local stratigraphic control of the T57 shale horizon.
Operations and results
Well 24/6-3 was spudded with the semi-submersible installation Deepsea Bergen on 18 April 2003. Drilling of the17 1/2" section was terminated at 253 m when the BHA became stuck in hole. Despite repeated attempts to free-off the BHA, the drill string was severed and the well temporarily abandoned for re-spud (well 24/6-4) some 20 m to the west of the original location. The well was permanently abandoned as a junk well after drilling of 24/6-4 was completed.
Testing
No drill stem test was performed.
No cuttings in this wellbore.
No cores in this wellbore.
No scanned core photos available
No palynological slides in this wellbore.
No oil samples available.
| Depth MD [m] | Mud weight [g/cm3] | Visc. [MPa.s] | Yield [pnt Pa.] | Mud type | Date measured |
|---|---|---|---|---|---|
| 155 | 1.05 | 20.0 | VISCOUS PILL | ||
| 206 | 1.05 | 20.0 | VISCOUS PILL |
No drill stem test in this wellbore.
No logs available.
| Top depth [m] | Litostratigraphic unit |
|---|---|
| 144 | NORDLAND GP |
No composite log presently available.
No geochemical data presently available. Regional geochemical studies which include data from this well may however be filed on a different well.
No documents presently available.