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Exploration wellbore: 6407/6-2

General information

NPDID wellbore: 522
Well name: 6407/6-2
Drilling operator name: Den norske stats oljeselskap a.s
Geodetic datum: ED50
Coordinates: 64° 42` 29.56`` N 7° 40` 32.59`` E
UTM coordinates: 7176774.36 N 436871.33 E
UTM zone: 32
Drilled in production licence: 092
Area: NORWEGIAN SEA
Drill permit: 484-L
Drilling facility:WEST VANGUARD
Drilling days: 3
Wellbore entry date: 04.10.1985
Wellbore completion date: 06.10.1985
Original wellbore purpose: WILDCAT
Wellbore purpose: WILDCAT
Wellbore status: BLOWOUT
Wellbore contents: GAS SHOWS
Discovery wellbore: NO
Seismic location: ST 8402 - 123 SP. 750
Kelly bushing elevation (KB) [m]: 22
Water depth [m]: 221
Total Depth (MD) [m]: 524
Final vertical depth (TVD) [m]: 504
Max inclination [°]:
Bottom hole temperature [°C]:
Oldest penetrated age: PLIOCENE
Oldest penetrated formation: NAUST FM
Note: All depths, except the water depth, are relative to kelly bushing (RKB)

Wellbore history

General

Well 6407/6-2 was drilled on a structure in the western part of the block. The structure has two distinct highs, and the target for this well was on the northern high. The primary objective for the well was to test possible hydrocarbon accumulation in sandstones of middle Jurassic age (Fangst Group). Secondary objectives were seen in sands near base Cretaceous (Cromer Knoll Group), in Early Jurassic sandstones (Tilje Formation), in sandstones within the Åre Formation, and in the Triassic Grey- and Red Beds. The top hole and Tertiary sections of this well were expected to contain shallow gas, possibly at a depth of 570 m. Possibly, also swelling, overpressured Early Eocene Red/Brown claystone could be encountered. The prognosed depth was 4150 m, or rocks of Triassic age.

Operations and results

Wildcat well 6407/6-2 was spudded with the semi-submersible installation West Vanguard on 4 October 1985. It was abandoned at a depth of 523 m due to a blow out. The blow out probably was caused by gas from a shallow sand pocket at 505 m. Gas samples from the blow out were analysed and found to be gas generated by bacteria at shallow depths.

The 20" casing had not yet been set so the blow-out preventer (BOP) had not been installed when the incident happened. At 20:50 hours in the evening an increase in the penetration rate from 40 to 700 m/hour was observed. Drilling was immediately stopped and the bit pulled out of hole. The hole was circulated for 35 minutes. A 3-m3 mud loss was observed. After gas had been circulated out drilling of a 12 1/4" pilot commenced from 508 m to 516 m. Here background gas again increased. After again circulating out the gas drilling continued to 524 m where the drill string was pulled out 15 m for a new stand connection. The well now started flowing uncontrolled and pumping of kill mud started. This did not stop the blow out. Gas flowed onto the deck of the rig and at 23:20 hours the gas exploded. One person was killed and the platform was severely damaged.

The well was suspended on 6 October 1985.

Testing

No drill stem test was performed.

Cuttings available at the NPD

No cuttings in this wellbore.

Cores available at the NPD

No cores in this wellbore.

Scanned core photos

No scanned core photos available

Palynological slides available at the NPD

No palynological slides in this wellbore.

Oil samples available at the NPD

No oil samples available.

Casing and leak-off tests

Type Casing diam. [inch] Depth below KB [m] Hole diam. [inch] Hole depth below KB [m] Lot mud eqv. [g/cm3]
CONDUCTOR 30 318.0 36 323.0

Mud

Depth MD [m] Mud weight [g/cm3] Visc. [MPa.s] Yield [pnt Pa.] Mud type Date measured
323 1.06 2900.0 11.0 WATER BASED 1985.10.07
524 1.08 2900.0 11.0 WATER BASED 1985.12.11

Drill stem test

No drill stem test in this wellbore.

Available logs

Log type Intervals logged [m]

Lithostratigraphy

Top depth [m] Litostratigraphic unit
243 NORDLAND GP
243 NAUST FM

Composite log

No composite log presently available.

Geochemical information

File 1 (Format:PDF. Size: 0.387 Mb )
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Documents reported by the licencees (period for duty of secrecy expired)

Completionreport (Format:PDF. Size: 0.914 Mb )
Completionlog (Format:PDF. Size: 0.167 Mb )
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Old NPD WDSS reports, NPD papers and other related documents

WDSS_General_Information (Format:PDF. Size: 0.197 Mb )
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