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| NPDID wellbore: | 912 | |
| Well name: | 6407/6-2 | |
| Drilling operator name: | Den norske stats oljeselskap a.s | |
| Geodetic datum: | ED50 | |
| Coordinates: | 64° 42` 29.56`` N | 7° 40` 32.59`` E |
| UTM coordinates: | 7176774.36 N | 436871.33 E |
| UTM zone: | 32 | |
| Drilled in production licence: | 092 | |
| Area: | NORWEGIAN SEA | |
| Drill permit: | 484-L2 | |
| Drilling facility: | ROSS ISLE | |
| Drilling days: | 13 | |
| Wellbore entry date: | 08.05.1986 | |
| Wellbore completion date: | 20.05.1986 | |
| Original wellbore purpose: | WILDCAT | |
| Wellbore purpose: | WILDCAT | |
| Wellbore status: | SUSP.REENTERED LATER | |
| Wellbore contents: | GAS SHOWS | |
| Discovery wellbore: | NO | |
| Seismic location: | ST 8402 - 123 SP. 750 | |
| Kelly bushing elevation (KB) [m]: | 22 | |
| Water depth [m]: | 221 | |
| Total Depth (MD) [m]: | 524 | |
| Final vertical depth (TVD) [m]: | 504 | |
| Max inclination [°]: | ||
| Bottom hole temperature [°C]: | ||
| Oldest penetrated age: | PLIOCENE | |
| Oldest penetrated formation: | NAUST FM | |
| Note: All depths, except the water depth, are relative to kelly bushing (RKB) | ||
General
Well 6407/6-2 R is a re-entry of the 6407/6-2, which was terminated at 524 m due to a blow out from a shallow gas zone. The purpose of the re-entry was plugging and permanent abandonment.
Operations and results
Wildcat well 6407/6-2 was re-entered with the semi-submersible installation Ross Rig on 8 May 1986.
The well was plugged back to 330 m before Ross Rig had to terminate operations and leave the locations for drilling well 7121/5-2 in the Barents Sea. The vessel Bucentaur would complete remaining plugging. The re-entry was suspended on 20 May 1986.
Testing
No drill stem test was performed.
No cuttings in this wellbore.
No cores in this wellbore.
No scanned core photos available
No palynological slides in this wellbore.
No oil samples available.
No mud data available.
No drill stem test in this wellbore.
No logs available.
| Top depth [m] | Litostratigraphic unit |
|---|---|
| 243 | NORDLAND GP |
| 243 | NAUST FM |
No composite log presently available.
No geochemical data presently available. Regional geochemical studies which include data from this well may however be filed on a different well.
No documents presently available.